Re: my small project
Wow, I can't believe you lifted that as one assembly, with the t-case attached. I had a hard enough time bench-pressing the t-case up off my chest, not to mention wrestling with the trans. Hey, if you need to borrow some 6-ton jackstands or a 3-ton jack, let me know. So I found out my turbo is toast today. Pulled the IC upper tube off and it was full of oil. The turbo shaft doesn't spin easily and has a good amount of sideways play in it. So I drove the truck around for about 20 minutes to burn out the oil that the turbo pumped into my motor and I thought I was golden until I got home. The exhaust started blowing thick white smoke, so it seems that I have a blown head-gasket? There was no obvious oil in the coolant or vice versa, so it must be a small leak. I pulled all of the plugs and they looked fine, except for the orange coating from the Torco. I was able to do compression checks only on cylinders 2, 3, 4, and 5 since 1 and 6 are blocked by the ATR headers. The compression on those four was 130, 122, 130, 135 respectively. Not sure about the other two cylinders, but the truck still idles perfectly and drives fine. It's just blowing white smoke from the exhaust. Any ideas? I'm thinking of buying a set of ported/polished Vortec heads and intakes and opening it up to see if it is indeed a head gasket. No idea why the RPM 60-1 turbo went bad after only 5K miles or so. This sucks...